This blog is a lab notebook for my work with the Reprap open source 3D printing undertaking.
Saturday, April 03, 2010
Delta 'bot Axis
It's one thing to design and print plastic parts that have to mate with steel rods. As I am finding it is quite another to design plastic parts that have to mate with other printed plastic parts. During the last week in my spare time I proved out a design for a hexagonal column which I think might accommodate a herringbone rack and a sleeve seating a pinion gear, stepper motor and two guide plates.
Heretofore, I have been butt seating the column sections and then post-tensioning them. While that was okay for demonstrating the design approach, worries about creep said that I needed to have a male/female attachment technology so that I could fit sections of the column together and avoid having them do a lateral creep out of alignment. That proved to be considerably more difficult than I imagined.
This last weekend, I decided to take a different approach and instead of doing a conventional slice and dice of an STL, I decided instead to work with the print roads of my thin-walled column instead. What I did is a radial 45 degree overhang inside the column onto which I printed the male insert. I think it is worth mentioning how I achieved that.
The column was achieved for most of it's length with three concentric print roads of 0.6 mm width. What I needed to do was to build a ledge inside the column. When I began the ledge I widened the innermost print road to 0.8 mm. On the next layer I replaced the 0.8 print road with two 0.6 print roads. This process left me a 0.2 mm miniledge onto which the new innermost print road could adhere. I repeated this process until I had a ledge wide enough to print the male insert onto.
You can see the insert successfully executed here.
I would like to be able to say that that was all an easy exercise. It wasn't. I did exactly thirty text prints like the one you see before I was satisfied with the seating of the guide strips, herringbone rack and the male/female column connector system. I also had to chase several heretofore unsuspected bugs in Slice and Dice AND extend the coding somewhat. All the same, it's done and works so far.
At that point, I decided to see how tall a monolithic column section I could print. It appears that Rapman three can handle about 225 mm in the z-axis. I designed a 200 mm column with a 4 mm male connector and am printing it at present.
It is 2120 and I am up to about 50 mm. I'm doing a 0.25 mm layer every 45 seconds, so I expect to be finished at about 0500 tomorrow morning.
With such a large print I began to encounter xy and z faults. The xy faults were annoying, but the z faults tended to plunge the hot extruder head into the print. Upgrading the Rapman firmware to 2.0.8 got rid of the z faults but the xy faults remained.
I reduced the column test print to 55 mm, relocated the Rapman further away from my PC on a table by itself away from the cold window and switched ABS to HDPE because the acrid fumes were getting to be too much when I wasn't able to open the windows.
A thorough cleaning of the extruder with compressed air was also undertaken. After a few test prints I got the flow rate sorted out for HDPE and was able to successfully print a 55 mm column section in HDPE.
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